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Simulated by grasping gripper attachment and applying light pressure for 30-60 seconds
Full Name: /Joints/Joint (wrist_flex_joint) Component: Joint (wrist_flex_joint) Hardware ID: 24 Level: STALE Message: Velocity integration error too large.(ExxxError/ControlDeviation); Firmware Version: 1f4dc1c93086356d52f5fed057dbbb0bcce461e9 Control Table Version: 6fe89466421b08f50b5bb06e59f1fb09 Connection Error Rate: 0 Command Position: -1.5700033769215975 Command Velocity: 0 Command Current: 0 Present Position: -1.9605833769215975 Present Velocity: -4.8000000000000001e-05 Present Effort: 0.1104 Present Temperature: 41 Present Current: 0.021000000000000001 Driver Type: 0
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Simulated by grasping gripper attachment and applying light pressure for 30-60 seconds
The text was updated successfully, but these errors were encountered: